Lean manufacturing implementation in an automotive assembly line / Nurul Hayati Abdul Halim
In this research the implementation of Lean Manufacturing (LM) system with an application of a set of lean tools in an automotive assembly area is examined. The study seeks to investigate how the lean mols could be applied and how the company could benefit from the implementation. In order to collec...
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الوصول للمادة أونلاين: | https://ir.uitm.edu.my/id/eprint/39796/1/39796.pdf |
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my-uitm-ir.397962022-04-07T04:58:07Z Lean manufacturing implementation in an automotive assembly line / Nurul Hayati Abdul Halim 2012-09 Abdul Halim, Nurul Hayati Manufacturing processes. Lean manufacturing In this research the implementation of Lean Manufacturing (LM) system with an application of a set of lean tools in an automotive assembly area is examined. The study seeks to investigate how the lean mols could be applied and how the company could benefit from the implementation. In order to collect data, the existing case study area called MYVI assembly line was examined and the current Material and Information Flow Charts (MIFC) was mapped. The purpose of mapping the present MIFC is to highlight the hidden waste in the existing system such as waiting times, transportation time and unwanted inventories. Based on this information, suitable lean tools such as set-up time reduction, continuous flow process and standardized work were identified and mapped accordingly in the future MIFC. The line balancing and re-layout activities complement the total LM system establishment. Through performance analysis, results from the implementation were measured and analysed by comparing the lean metrics between the existing conditions against the improved system. The performance of the improved system were then presented in the form of productivity and cost saving. The findings revealed that the company managed to increase their productivity and reduce the operational cost significantly after the LM implementation. It can be concluded that a systematic approach is essential and appropriate lean tools is crucial for the LM establishment process. Based on the findings, it was recommended that the management replicate these activities in other assembly areas or manufacturing areas in order to achieve full LM system company wide. 2012-09 Thesis https://ir.uitm.edu.my/id/eprint/39796/ https://ir.uitm.edu.my/id/eprint/39796/1/39796.pdf text en public masters Universiti Teknologi MARA Faculty of Mechanical Engineering Jaffar, Ahmed (Professor Ir. Dr. Hj.) |
institution |
Universiti Teknologi MARA |
collection |
UiTM Institutional Repository |
language |
English |
advisor |
Jaffar, Ahmed (Professor Ir. Dr. Hj.) |
topic |
Manufacturing processes Lean manufacturing |
spellingShingle |
Manufacturing processes Lean manufacturing Abdul Halim, Nurul Hayati Lean manufacturing implementation in an automotive assembly line / Nurul Hayati Abdul Halim |
description |
In this research the implementation of Lean Manufacturing (LM) system with an application of a set of lean tools in an automotive assembly area is examined. The study seeks to investigate how the lean mols could be applied and how the company could benefit from the implementation. In order to collect data, the existing case study area called MYVI assembly line was examined and the current Material and Information Flow Charts (MIFC) was mapped. The purpose of mapping the present MIFC is to highlight the hidden waste in the existing system such as waiting times, transportation time and unwanted inventories. Based on this information, suitable lean tools such as set-up time reduction, continuous flow process and standardized work were identified and mapped accordingly in the future MIFC. The line balancing and re-layout activities complement the total LM system establishment. Through performance analysis, results from the implementation were measured and analysed by comparing the lean metrics between the existing conditions against the improved system. The performance of the improved system were then presented in the form of productivity and cost saving. The findings revealed that the company managed to increase their productivity and reduce the operational cost significantly after the LM implementation. It can be concluded that a systematic approach is essential and appropriate lean tools is crucial for the LM establishment process. Based on the findings, it was recommended that the management replicate these activities in other assembly areas or manufacturing areas in order to achieve full LM system company wide. |
format |
Thesis |
qualification_level |
Master's degree |
author |
Abdul Halim, Nurul Hayati |
author_facet |
Abdul Halim, Nurul Hayati |
author_sort |
Abdul Halim, Nurul Hayati |
title |
Lean manufacturing implementation in an automotive assembly line / Nurul Hayati Abdul Halim |
title_short |
Lean manufacturing implementation in an automotive assembly line / Nurul Hayati Abdul Halim |
title_full |
Lean manufacturing implementation in an automotive assembly line / Nurul Hayati Abdul Halim |
title_fullStr |
Lean manufacturing implementation in an automotive assembly line / Nurul Hayati Abdul Halim |
title_full_unstemmed |
Lean manufacturing implementation in an automotive assembly line / Nurul Hayati Abdul Halim |
title_sort |
lean manufacturing implementation in an automotive assembly line / nurul hayati abdul halim |
granting_institution |
Universiti Teknologi MARA |
granting_department |
Faculty of Mechanical Engineering |
publishDate |
2012 |
url |
https://ir.uitm.edu.my/id/eprint/39796/1/39796.pdf |
_version_ |
1783734540692357120 |