Productivity improvement for visual inspection using lean concept a case study at front of line process

Nowadays,semiconductor manufacturing companies aim for higher productivity with short lead time that will maximize the profit to the organization for their survival. This project is conducted at Infineon Technologies(M)Sdn.Bhd. especially at Front of Line area that focusing on quality performance of...

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Main Author: Augustine, Noel Francisco
Format: Thesis
Language:English
English
Published: 2016
Subjects:
Online Access:http://eprints.utem.edu.my/id/eprint/20453/1/Productivity%20improvement%20for%20visual%20inspection%20using%20lean%20concept%20%20a%20case%20study%20at%20front%20of%20line%20process.pdf
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spelling my-utem-ep.204532022-12-28T16:39:51Z Productivity improvement for visual inspection using lean concept a case study at front of line process 2016 Augustine, Noel Francisco T Technology (General) Nowadays,semiconductor manufacturing companies aim for higher productivity with short lead time that will maximize the profit to the organization for their survival. This project is conducted at Infineon Technologies(M)Sdn.Bhd. especially at Front of Line area that focusing on quality performance of visual inspection for die bond and wire bond processes. There are redundant quality visual inspection activities between Production operators and Process Control operators.Here, the production operators whom operate the machines while Process Control operators whom conducting quality surveillance checks perform similar quality visual inspection. Furthermore, there is inconsistent duration of visual inspection activities although the standard work instruction has been provided. Therefore, the aim of the project is to improve the productivity of visual inspection process through elimination of non-value activities at Dpak package Front of Line process by 50%. There are three objectives defined for this project; (i) to identify the NV A and NVA but necessary activities using time study, (ii) to determine root cause of NVA and NVA but necessary and perform simulation with proposed action and (iii) to validate the proposed solutions through implementation of actions for improvement. Time study and brainstorming has been used in order to achieve objective one. Then, the root causes of the NVA and NVA but necessary had been determined using 5 Why's tool. Actions for improvement were proposed and simulated.Finally, the proposed actions for improvement are validated by reduction of total time taken for visual inspection activities. As a result,the total time of visual inspection activities has been reduced for 50% to 70% in which before improvement, total 40% of the total time caused by NVA and NVA but necessary activities.ln conclusion, eliminating NVA and NVA but necessary activities can increase productivity by reduction of process time. 2016 Thesis http://eprints.utem.edu.my/id/eprint/20453/ http://eprints.utem.edu.my/id/eprint/20453/1/Productivity%20improvement%20for%20visual%20inspection%20using%20lean%20concept%20%20a%20case%20study%20at%20front%20of%20line%20process.pdf text en public http://eprints.utem.edu.my/id/eprint/20453/2/Productivity%20improvement%20for%20visual%20inspection%20using%20lean%20concept%20a%20case%20study%20at%20front%20of%20line%20process.pdf text en validuser https://plh.utem.edu.my/cgi-bin/koha/opac-detail.pl?biblionumber=104948 mphil masters Universiti Teknikal Malaysia Melaka Faculty Of Manufacturing Engineering Ebrahim, Zuhriah
institution Universiti Teknikal Malaysia Melaka
collection UTeM Repository
language English
English
advisor Ebrahim, Zuhriah
topic T Technology (General)
spellingShingle T Technology (General)
Augustine, Noel Francisco
Productivity improvement for visual inspection using lean concept a case study at front of line process
description Nowadays,semiconductor manufacturing companies aim for higher productivity with short lead time that will maximize the profit to the organization for their survival. This project is conducted at Infineon Technologies(M)Sdn.Bhd. especially at Front of Line area that focusing on quality performance of visual inspection for die bond and wire bond processes. There are redundant quality visual inspection activities between Production operators and Process Control operators.Here, the production operators whom operate the machines while Process Control operators whom conducting quality surveillance checks perform similar quality visual inspection. Furthermore, there is inconsistent duration of visual inspection activities although the standard work instruction has been provided. Therefore, the aim of the project is to improve the productivity of visual inspection process through elimination of non-value activities at Dpak package Front of Line process by 50%. There are three objectives defined for this project; (i) to identify the NV A and NVA but necessary activities using time study, (ii) to determine root cause of NVA and NVA but necessary and perform simulation with proposed action and (iii) to validate the proposed solutions through implementation of actions for improvement. Time study and brainstorming has been used in order to achieve objective one. Then, the root causes of the NVA and NVA but necessary had been determined using 5 Why's tool. Actions for improvement were proposed and simulated.Finally, the proposed actions for improvement are validated by reduction of total time taken for visual inspection activities. As a result,the total time of visual inspection activities has been reduced for 50% to 70% in which before improvement, total 40% of the total time caused by NVA and NVA but necessary activities.ln conclusion, eliminating NVA and NVA but necessary activities can increase productivity by reduction of process time.
format Thesis
qualification_name Master of Philosophy (M.Phil.)
qualification_level Master's degree
author Augustine, Noel Francisco
author_facet Augustine, Noel Francisco
author_sort Augustine, Noel Francisco
title Productivity improvement for visual inspection using lean concept a case study at front of line process
title_short Productivity improvement for visual inspection using lean concept a case study at front of line process
title_full Productivity improvement for visual inspection using lean concept a case study at front of line process
title_fullStr Productivity improvement for visual inspection using lean concept a case study at front of line process
title_full_unstemmed Productivity improvement for visual inspection using lean concept a case study at front of line process
title_sort productivity improvement for visual inspection using lean concept a case study at front of line process
granting_institution Universiti Teknikal Malaysia Melaka
granting_department Faculty Of Manufacturing Engineering
publishDate 2016
url http://eprints.utem.edu.my/id/eprint/20453/1/Productivity%20improvement%20for%20visual%20inspection%20using%20lean%20concept%20%20a%20case%20study%20at%20front%20of%20line%20process.pdf
http://eprints.utem.edu.my/id/eprint/20453/2/Productivity%20improvement%20for%20visual%20inspection%20using%20lean%20concept%20a%20case%20study%20at%20front%20of%20line%20process.pdf
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